Hey everyone,
I'm working on tuning my '75 Yamaha DT400 (2 stroke single). Stock jetting is #40 pilot, #160 main on a Mikuni VM32 round slide carb.
I have the stock airbox (with a UNI filter), and an aftermarket pipe.
On the pilot side, I went rich because I am new to this and have no idea how changing the exhaust impacts jetting. Started with 55 pilot, 185 main. Huge amount of four stroking, massive amounts of spooge coming out of the exhaust. Ran like crap, wouldn't idle, no need for a choke. So, way rich. Pilot air screw did nothing
Take two, 45 pilot, 185 main. Still massively rich, spooge everywhere. Pilot air screw was no help
Ok, take 3. Pulled the carb, double checked float height, went to stock jetting (40 pilot, 160 main). Fire it up. Ok, it held an idle now, still rich (I think). Pilot air screw didn't seem to do much
Ended the day at 30 pilot, 160 main. It finally stopped four stroking on idle, and it started feeling and sounding more like it should (I think, based on no experience). My gut is telling me it is still rich on the pilot circuit. Maybe a 25 pilot is needed? Ran a sweep of the pilot air screw from closed to open, didn't find a sweet spot really.
If I blip the throttle from idle to about 1/3, it takes a while to come back down. Sounds like its four stroking. As I blip it, it rolls on good and sounds pretty crisp. Then I shut the throttle and it can hang there for a bit, still firing, then slowly starts to fall while four stroking (or what sounds like four stroking to me). Not sure what this hanging is - seems like fuel is getting in there to sustain the combustion.
My question is - is it common to have to dive this far UNDER stock jetting? I always ran under the assumption that, if you improve airflow, you may have to richen the mixture. My exhaust, I am assuming, improved airflow. So I'm wondering what's going on.
Anyway. I'm still trying to get the pilot circuit right before I move on to the needle and main, just need a little guidance.
Also - the engine was tested for leaks before it went into the frame. It held 7psi for 10 minutes or so. I guess its possible an air leak has developed since then, but it was airtight when the engine went in.
I'm working on tuning my '75 Yamaha DT400 (2 stroke single). Stock jetting is #40 pilot, #160 main on a Mikuni VM32 round slide carb.
I have the stock airbox (with a UNI filter), and an aftermarket pipe.

On the pilot side, I went rich because I am new to this and have no idea how changing the exhaust impacts jetting. Started with 55 pilot, 185 main. Huge amount of four stroking, massive amounts of spooge coming out of the exhaust. Ran like crap, wouldn't idle, no need for a choke. So, way rich. Pilot air screw did nothing
Take two, 45 pilot, 185 main. Still massively rich, spooge everywhere. Pilot air screw was no help
Ok, take 3. Pulled the carb, double checked float height, went to stock jetting (40 pilot, 160 main). Fire it up. Ok, it held an idle now, still rich (I think). Pilot air screw didn't seem to do much
Ended the day at 30 pilot, 160 main. It finally stopped four stroking on idle, and it started feeling and sounding more like it should (I think, based on no experience). My gut is telling me it is still rich on the pilot circuit. Maybe a 25 pilot is needed? Ran a sweep of the pilot air screw from closed to open, didn't find a sweet spot really.
If I blip the throttle from idle to about 1/3, it takes a while to come back down. Sounds like its four stroking. As I blip it, it rolls on good and sounds pretty crisp. Then I shut the throttle and it can hang there for a bit, still firing, then slowly starts to fall while four stroking (or what sounds like four stroking to me). Not sure what this hanging is - seems like fuel is getting in there to sustain the combustion.
My question is - is it common to have to dive this far UNDER stock jetting? I always ran under the assumption that, if you improve airflow, you may have to richen the mixture. My exhaust, I am assuming, improved airflow. So I'm wondering what's going on.
Anyway. I'm still trying to get the pilot circuit right before I move on to the needle and main, just need a little guidance.
Also - the engine was tested for leaks before it went into the frame. It held 7psi for 10 minutes or so. I guess its possible an air leak has developed since then, but it was airtight when the engine went in.